The Forestry Forum

General Forestry => Forestry and Logging => Topic started by: RKH Logging on June 15, 2014, 06:36:18 PM

Title: pulled the motor today
Post by: RKH Logging on June 15, 2014, 06:36:18 PM
Well i got the engine out today. Took 4 hours with me and a helper. Still havent decided where its going to be fixed. Was thinking of tackling it myself.

 (https://forestryforum.com/gallery/albums/userpics/35472/20140615_122757.jpg) 

 (https://forestryforum.com/gallery/albums/userpics/35472/20140615_170511.jpg) 

 (https://forestryforum.com/gallery/albums/userpics/35472/20140615_182605.jpg)
Title: Re: pulled the motor today
Post by: clww on June 15, 2014, 08:30:45 PM
What's wrong with the engine?
Title: Re: pulled the motor today
Post by: Dave Shepard on June 15, 2014, 09:33:32 PM
Find the 4-53 thread (https://forestryforum.com/board/index.php/topic,75642.0.html) here.
Title: Re: pulled the motor today
Post by: BargeMonkey on June 15, 2014, 09:51:05 PM
 I went down this road with my 230. Bite the bullet and stuff a 4-BTA in the machine, my 405 had one and it was such a nice machine, and didnt eat alot of fuel. There are lots of them out there, straight mechanical engine, actually would take up less room.
Title: Re: pulled the motor today
Post by: Dave Shepard on June 15, 2014, 09:54:42 PM
I'm having issues with the 3-53 in the 208, and if I had the money, I would put a 4BT in there. So much quieter. ;D
Title: Re: pulled the motor today
Post by: BargeMonkey on June 15, 2014, 10:00:31 PM
Quote from: Dave Shepard on June 15, 2014, 09:54:42 PM
I'm having issues with the 3-53 in the 208, and if I had the money, I would put a 4BT in there. So much quieter. ;D
I think it can be done for about 3500 with a good used one, ive seen a few new long blocks bare engine for 5k. Less noise, less drama. Im down to 2 detroits left in the fleet, and after that no more. You can hear my forwarder 5 miles away on a clear day. In their day they where a great engine, tons of them still out here in the maritime world.
Title: Re: pulled the motor today
Post by: Dave Shepard on June 15, 2014, 10:02:06 PM
I am a big fan of Cummins engines, but have developed a respect for the Detroits. They're just outdated, especially the noise part. :D
Title: Re: pulled the motor today
Post by: BargeMonkey on June 15, 2014, 10:17:06 PM
 The reason behind the noise is due to the engine being 2 stroke. Your valve train and gear train is 90% of it. In a 2 stroke its 1-1 speed to rpm, in a 4 stroke your 1/2 the rpm speed for the gear train. Hope I explained that right. Did a 3 day detroit program in Ft Lauderdale about 10 yrs ago.
Title: Re: pulled the motor today
Post by: Dave Shepard on June 15, 2014, 10:18:36 PM
Oh, I know why it's loud. I do like the sound of a 12v71 opened up all the way. ;D
Title: Re: pulled the motor today
Post by: barbender on June 17, 2014, 12:41:19 AM
The how come don't matter, I just know they sound UGLY :o I used to think they sounded cool when I was a kid, and they still have a nostalgic effect. However, whenever I spend more than an hour on my 353 powered skidder sometimes I dream of it blowing up so I can justify throwing a 4bt Cummins in it ::) The problem is, my Detroit is tight, and although I don't care for the Detroit "dirt bike" power curve, the things are pretty darn bullet proof and they sip fuel for the amount of power they have.
Title: Re: pulled the motor today
Post by: Corley5 on June 17, 2014, 08:11:10 AM
I've got to pull the Deutz out of my C4 forwarder in the very near future.  We've limped it along with its weak clutch and leaking seals in the bell housing to get this job done.  We should be done today  8)  I'd rather log than wrench but wrenching is part of logging  ;D
Title: Re: pulled the motor today
Post by: Autocar on June 17, 2014, 10:45:41 AM
Ive always wore hearing protection other wise when I came home all I could hear was the screaming detorit.
Title: Re: pulled the motor today
Post by: tantoy on June 17, 2014, 11:15:17 AM
I would clean, degrease, pressure wash the motor good and then pull the exhaust manifold and then pull the head. If the problem isn't obvious, then take the head and have it magnafluxed to check for cracks.Probably has a cracked head allowing coolant into one of the pistons and then flowing out the intake ports into the air box.